Older News (2013)

May 21, 2013: Engine is warm, the thermosiphon from the hot water heater to the engine was active. This means that the coolant loop to the hot water heater does not have any air in it. Still no moisture on the front of the engine. Before shower the sump under the seat in the aft head was completely dry. After a careful shower there was perhaps a tablespoon of water (half a paper towel). Wiped up. Definitely appears to be comming from either the forward fittings going to the shower head or the hose itself leaks under just the right bend. At least it appears to be a readily fixable problem. Will continue to monitor.

May 20, 2013: Evening check of the engine, no moisture on the paper towels on the front of the engine. Looks like tightening up the hose clamps was sufficient for now to stop the leaks.Turned on the hot water heater to verify that the warming from the hot water heater was not the issue.

May 19, 2013: General in the slip maintenance, there was a asmall amount of antifreeze which has shown up between the generator and the main engine. A paper towel at each end of the rubber connection between the circulating pump and the header tank was found to be damp with antifreeze after several days.

One of the two hose clamps could be tightened a little over one turn, the other only about 1/4 turn. Warming up the engine to allow it to cool down under pressure and see if the seap shows up again.  Definitely one of the only remaining (perhaps the only) original hoses on the engine. I will plan to replace that hose in the fall if it seals up for now. Probably the easiest way to replace the hose is to pull the circulating pump. If it is off the engine, I might as well have it rebuilt.

General cleaning during the week found a bit of water under the forward bunk, port side, can be felt by pulling the drawer under the bunk and reaching over the central stringer. Most likely was the result of the slightly leaking hatch above the bunk and some really rough weather. Will continue to monitor.

Found water under the shower seat is in the aft head. I had taken a shower so it may be related, will continue to monitor.

Replaced the desecant bags all through the boat in lockers. These do seem to make a significant impact without having to run a dehumidifier all of the time.

Engine running with all of the covers off at fast idle to warm up. Engine sounds very good and very smooth. Transmission is very quiet in neutral, thus the noises when out of gear when I bought the boat were not normal contrary to what the engine surveyor (at time of purchase) suggested.

Not running the blowers with the covers off to be able to best hear the sounds of the engine.

Definitely a good look at the hose, the other end is on the circulating pump so the easiest way to replace the hose would be to pull the circulating pump.

Engine HRS: 998.4 (0.5 hrs)

Tx Hrs since last change 3.9hrs

Tightened up alternator belt (has been a bit loose for my taste for some time) needed a 10mm wrench to loosen the arm.

Note that the sticky substance on the fuel lines under the alternator appears to be coming off the bottom of the alternator (near the internal regulator). It might be related and could be an indication of alternator issues.

Ran engine for a few minutes, no apparent issues with either the tightened belt or the tightened hose clamps on the circulating pump hose. Engine is in lock out/tag out until I pull the paper towles off the critical points but otherwise ready to go.

May 6, 2013: Maintenance found about two papertowels of yellow antifreeze in well between main engine and generator. May be the overflow tank hose connection leaking, tightened up connection and inspected closed circuit cooling pump on engine and hoses on front of engine. All appear to be intact.

Definitely antifreeze on hose bundle which has coolant recovery tank and the hot water heater connection off the header tank. Could easily be either. Will monitor to be sure that the connection to the header tank was actually the issue and not the connection to the hot water heater..

Bilge water is tan clear colored. Had added bilge cleaner two weeks ago. May just be some of what the cleaner removed. Could also be part of the water which showed up by the shaft seal. Will empty bilge, flush with fresh water and monitor.

May 5, 2013: Leaving Avalon 1245 pm, heading for home.Motored for 10 min out of harbor and then was able to sail. Arrived back in King Harbor at 1830 (5.25 hr)

Note, sailed significant wing on wing as a test. below about 18 knts the polars are about 10 percent hot. above 22 knts they are about right. Otherwise the 120 to 160 polars look pretty good from 14 knts to 24 knts.

Updated polars to take off 10% of the ddw values for speeds below 18 knts of true wind to reflect what we saw running wing on wing. Perhaps a bit pessamistic but this is the first real data over an extended period trying DDW.

No water under shaft seal upon return home; Engine hr 997.9; Tx oil hr 3.3; gen hr 3184.9 (current oil hr is approx 13).

May 4, 2013: Departed 0900 Avalon, sailing at 7 knts just out of harbor on main and staysail., sailed 2/3 way to r10. Cleared r10 now hard on wind making 180M at 5 knts with tws of 16 knts will have to tack nearing island.

The winds mid channel are pretty significant: bs 6.13; awa 60; tws 19; aws 20; sog 5.8; cog 174; heading 176; set 17 drift 0.4. Working with the main and staysail only.


The sea state was pretty rough with short chop out of the south. In the end, I should have headed for Isthmus and then motor sailed up the backside of Catalina and it would have been a more comfortable trip all around. Pulled into Avalon and picked up mooring 212 at 1530. Engine hr 996.5; Tx fluid 1.9hr.

Odd, there is some water under the shaft seal. Does not look like it came from the seal, slightly brownish. May have been standing water from somewhere which got through. Perhaps from the rudder shaft seal. Cleaned up, about two paper towels worth. Shaft seal is dry. Will monitor on return.

Verified that there is no moisture under the aft bunk. Rudder shaft area looks normal. Perhaps the large seas pushed some water up through the rudder shaft seal which ended up in the shaft seal bilge area.

Determined after the fact that the reason that the computer would show 50% of expected performance is that the upper wind velocities were not re-programmed for this boat and were very high. Once over the correct values, interpolation would take over resulting in surprising readings.

May 3, 2013: Trip to Avalon with the Grubers, Cameron & Emily. Everyone came aboard on Friday evening for a nice run to the island. Engine hr 994.6; Tx fluid 0hr; generator hr 3184.1 (intermittent generator hour meter) current oil hr is 12.

May 2, 2013: 5.2.2013 Forward head rebuild work underway. The painting is finished, was able to reroute the plumbing to have the sink drain working.

April 30, 2013: Second coat of white bilge cote applied at 1900 on Tuesday. Prior coat was very hard and sanded with a course scotch bright very nicely.

This coat, like the last, I worked the low spot to make sure that paint did not puddle in the corner next to the hull which is the low spot. I used a dry brush to very lightly brush out of the puddle area onto the flat, as long as 3 hours after painting at 50 degrees the paint appears to be flowing out nicely without significantly impacting the finished look.

Data from tank fill in Marina Del Ray (964.5hrs) just after going back into the water:

Note that the bottom of the marks on the dip tube was about 6" of fuel in the tank. There are marks every inch on the stick from there and they agreed well with the Hart Systems guage:

Gallons              2-3 inches remain on stick

Added  Hart        Stick
0              6"        Bottom Mark
10           7.5"      2 1/2
20           9"           
30           11"
40           12"
50           13"
60           14.5"
70           15.25"
80           16.5"
90           17.5
100         18.25"
110         19.25"
120         20.25"
130         21.25"

Engine run is 30 hours since fill up (12 hr on generator).

Consumption is about 35 gallons, if assume 1/4- 1/2 gal/hr on gen that would be 3 -5 gallons for generator and about 30 gallons for engine or about 1gal/hr but at most 1.1 gal/hr.

April 28, 2013: The weather at breakfast looked so nice that Glen R and I decided to go for a day sail up to Malibu and back. It was a glorious day. We left the dock at 1130, were off Malibu at 1400, put some pizza in the oven for snacks on the way heading back toward Palos Verdes and was back in the slip at 1615. It took about half an hour to clean the boat up.  

Boat information: Engine hours 994.6; 0.75 hr on tx fluid; 28.6 hr on motor oil; no generator time; fuel at 18" at completion of trip

First coat of white bilge cote applied at 2345 on Sunday. Depending on temperature it needs to be overcoated in 2 to 3 days.

Used a course scotch bright to sand surface. Vacuumed with no chemical wipe prior to painting.

April 27, 2012: Ran engine for 15 minutes, took transmission sample, changed transmission oil. Unit fill to ring on dipstick with threads not engaged.

Replaced bilge pads, small dots of fluid on pad one where shift leaver comes out of the transmission, one where the tip of the shift leaver is when in the down position. Perhaps three drips of fluid in 5 hours of runtime. This is somewhat expected with the new/old stock transmission, luckily the output seals are not dry. Not worth the trouble to change, especially with the short run time on the transmission recommended by blackstone.

Total fill on the transmission is 28oz, (i.e. 4 oz left in the bottle. This is consistent with the manual stating that the transmission requires 7/8 quart of fluid.

Plan is to replace fluid about every 25 hours and sample as the transmission wears in and then work toward an extended period of time once the values are stable.

Forward head rebuild in process. Tried to re-gelcoat and surface contamination is a problem in this area also. In the future just go straight to interlux "pre-kote" and then a couple of coats of "bilge coat"

Was able to pull apart seat in head without damage, will re-work with fresh Formica.

Aft shower is back online.

April 22, 2013: Found dirty water in the aft shower under seat. Not clear where it came from, looks like there was some sludge on stringer which got wet and then ended up in the water. All cleaned up, will monitor.

Pulled toilet off base and verified no leaks. Need to add access panel to baseboard to ensure I can get in there to clean up water if cleaning fluid was spilled or the toilet leaked.

April 14, 2013: Heading home after the work party. Emerald Bay is beautiful as is often the case this time of year.

Pre-Sail check: 18.5 inches fuel; 989.9 hrs engine; 3183.9 hrs on generator (no run for the weekend); Engine oil level looks good. Transmission fluid good (note two drops on pad, one for arm, one for piviot). Coolant is good in the engine, needs a cup added to the recovery tank; Batteries are down -88ah on main bank, bank is 440ah or about 20% down.

1250 Main engine up and sounds good. Good water flow.

1255 Time to depart Emerald Bay pulled away from the mooring. Motoring due to lack of wind

bs 6.9 hd 14 sog 7.7 cog 12 set 355 drift 0.79

bs 7.0 hd 14 sog 7.4 cog 13 set 320 drift 0.7
bs 3.3 hd 6 sog 3.4 cog 12 set 100 drift 0.52
bs 4.7 hd 8 sog 4.8 cog 12 set 80 drift 0.71
bs 5.8 hd 5 sog 5.9 cog 9 set 100 drift 0.6
bs 6.1 hd 5 sog 6.1 cog 10 set 100 drift 0.6
bs 6.8 hd 11 sog 7.2 cog 13 set 40 drift 0.5

near R10 Bouy

bs 7.1 hd 14 sog 7.6 cog 13 set 30 drift 0.55

1530 cleared R10 bouy

bs 6.9 hd 20 sog 7.8 cog 22 set 12 drift 1.02


getting close to the redondo beach breakwater

bs 6.9 hd 23 sog 8.0 cog 35 set 66 drift 0.99

bs 6.9 hd 31 sog 7.9 cog 32 set 38 drift 0.99

Back in slip 1615hrs

dingy and anchor off 1630 hrs

Engine 993.5 hrs (27.5 hrs on oil); Generator 3183.9 (intermittent) (11.5 real hours this oil change); transmission 27.5 hours on tx fluid

Coolant in recovery tank on main engine was slightly low. The recovery tank was empty when I checked it cold, pulled cap and it was full. Added 2 cups of 50/50 antifreeze to the recovery tank. Hopefully will not be too full when hot. System probably burped some air from the running over the weekend. No signs of any leaks.

Usual minor amount of moisture under the shaft seal. Wiped dry, did not dampen a paper towel significantly.

Normal couple of drops of transmission fluid on pad under engine. One for the shifter shaft, the other for the tip of the shift leaver which is pointed downward when in gear. This is probably a couple of drops in a 3 hour run. Probably the concern of these transmissions when they sit on the shelf too long and the seals dry out. No apparent input or output seal issues.

Will order sample kits and it is about time to sample the transmission again and change the oil (it is over 25 hours). Due to the just right sized transmission, changing the transmission fluid (less than a quart) twice as often as the engine probably makes sense until blackstone labs says otherwise.

Fridge and freezer held over from 6pm friday night to sunday 5pm and frost on all three plates still fully frozen. No fridge run over the weekend.

Back at the dock at -66ah. The alternator on the main engine can keep up with the current demands and still put some back in but it is not significant. Once the new inverters and hardware are installed I will have to look at what can be done to install a larger alternator.

April 13, 2013: Work party in the cove. No run of engine or generator.

April 12, 2013: Heading over to Emerald Bay for the first Corsair Yacht Club work party of the season.  Not much wind, motor sailed the entire passage.

Pre-Sail Check: Engine hr 986.3, engine oil good, transmission oil good.; fuel load 19.0 inches

Departed slip 1825hrs


bs 6.42 hd 205 sog 6.5 cog 205 set 274 drift 0.19

Arrived at R10 Bouy 1920hrs

1925 9knts true winc 7.1 sog

Near Catalina Island, no moon, Nav system had trouble, rebooted and would not come up correctly (failure to start) appears to be related to having been in nighttime mode when the system was shut down.

Had to run the "clean menus" executable and then copy the raytech.ini file back into the windows directory and all of the instruments were restored. Will make further notes on this in the future.

2015 On mooring in Emerald Bay. Remaining fuel load 18.5 inches;  Hour meter shows 989.9 hrs on main engine.

April 11, 2013: Preventative maintenance
PM - running engine 1 hr in gear to verify that the cooling system is in good shape after the rework of early in the week.
Start at 985.3 hrs (0.3 hr on Monday to show no leaks and be sure fill is good). After warming up the engine ran loaded in gear. Cycled open hot water heater circuit for 10 minutes to clear old antifreeze out of that loop and ensure that the valves still work.

April 8, 2013: Took end plate to S&W Diesel in Wilmington CA. Purchased two complete heat exchanger gasket sets, one set for putting back together the current rework and one set for spares aboard. One set of gaskets is about $30.

Perkins Part Numbers:

O-Ring for end plate near exhaust mixer: 2415836 with "SSM" on package ($4.25)

Round Gasket for end plate near oil cooler, inside stack: 24865062 with "ST2" on package ($11.85)

Round Gasket with cross piece for end plate near oil cooler: 24865061 with "SUP" on package ($11.85)

Note: The line drawing in the manual appears to have the seals reversed with the O-Ring near the oil cooler and the other two at the far end plate near the exhaust mixer. Unfortunately this cannot be the case as the cross piece keeps the inlet and outlet water seperate as it is a back and forth stack set. I will have to take pictures next time I have it apart.

Due to finishing up at work early, I drove back down to S&W to pick up the drilled part. Don was still working on it and invited me to look around the shop. They had a 4.108 on the dyno out back being load tested. Don was able to drill out the old plug and get a tap to chase down the original threads getting this piece as good as new. After a trip through the media blaster it looked like new! The old plug looked like it was a solid plug rather than with treads for a zinc pencil. The old part might have been a brass plug rather than bronze but at any rate suffered de-zincafication with the orange/red color prominant at the failure point. Don recommended replacing with a Zinc Pencil. Others have suggested putting back in a new bronze plug. I will research but I have a zinc pencil in there at the moment:

West Marine: 3/8 x 1 3/4. WM 332155 ($2.84)


However, I am not sure that is the right one. I thought a 3/8 pipe plug was one size too big so it is possible the parts were mis marked.

Re-installed the end plate with a new o-ring on the exhaust mixer end. Wet the o-ring with a small amount of silicone plumbers lubricant. Tightened to snug but not overly tight.

Installed zinc pencil holder with a small amount of permatex type 2 non-hardening thread sealant.

Installed coolant side drain in heat exchanger with permatex type 2 non hardening thread sealant.

Refilled coolant with 50/50 solution of Peak Long Life for mixing with any color of coolant.  This is ethylene glycol based coolant which I use in both the engine and the generator.

The Perkins M90 needs just under 2.5 gallons of coolant if drained from the plug in the bottom of the heat exchanger and a shop vac used to pull any remaining coolant (very little but tends to have the last of the coolant loop contamination in it). Filling the coolant system from the header tank appears to result in a full system without air locks. I just run the engine up to temperature, verify excess coolant ends up in the recovery tank and then add about 2 cups of coolant to the recovery tank and result in a full system.

It appears that exchanger 2486586 is similar to what I have but with the drawing (CD-ID: SPI2_v2010A) having the gaskets reversed between the two end plates. In this drawing there are either petcocks or plugs in the two drains (coolant and raw water) and no indication of a zinc being used. I will continue to persue if there should be a zinc in the heat exchanger or not.

Ran engine up to temperature and allowed to cool complete. It looks like there are no leaks. I will plan to run the engine up to temperature one more time before leaving the slip.

Engine notes:

Upper plate on exhaust manifold (alternate position for mixer covered with plate) is showing some signs of minor salt corrosion around the mating surfaces. Top seal on oil cooler is showing some signs of minor salt corrosion around the mating surfaces.

Both of these items were in the shop last summer (6/2012) for general working through and these connections were definitely serviced. Both Bob and Don at S&W recommend taking these apart for cleaning and removing corrosion every two years due to the very high cost of having to replace these exchangers if corrosion gets away from you.

Alternator belt is too loose, need to replace and re-adjust. Not using a high output alternator at this point so tension is not as critical.

Spare heat exchanger gaskets and zinc pencil are under port floor in aft stateroom.

The bilge pads under the engine are definitely doing their job now, the level of random leaks is sufficiently small that any discoloration on the pad is cause to start chasing the problem and get it solved early.

There is one place on the stbd side of the engine (heat exchanger side) where getting the outboard bilge completely clean is difficult. that still needs worked.

Definitely need to rebuild or replace the stainless water lift soon. There are now two very minor weaps on the first weld going into the water lift. Plan to pull after the next trip to Catalina and send out for rework.

April 7, 2013: Applied heat shrink to the antenna of the GPS Rapid fix beacon (the one which I purchased for the trip to Kwaj. The self test passed.

The beacon which came with the boat was purchased in 1995. It still passes self test. It is still registered in the prior owners name. I am going to have to call and get it registered to me so I can update its information.

Pulled the mixing faucets for the forward shower to get access the varnish which is getting water under it. Ideally I will replace with a temperature controlling mixing valve assembly. the current center to center distance issix inches or slightly more.

Going up to West Marine for a battery holder for the stove, look at switches for the propane system, and a hose clamp for the exhaust.

Hose clamps for the exhaust found, 48mm parts. Installed, 1.50 each

Found battery holder at radio shack and installed on stove with double stick tape, still need surface mount on/off switch for the propane sensor.

Tightened drain plug on back of heat exchanger to stop very slow leak. Head of plug broke off 1/4 turn tighter.  Red / Pink corrosion at the point where it came apart. Drained antifreeze and closed engine seacock. Pulled Engine battery switch for lock out. Pulled end plate. It will need drilled out. I could probably do it with a hand drill but I will take it down to S&W and have them get it out. A Replacement end plate is about $400 - $500, let S&W do it with the proper tools!

April 6, 2013: Using the above swing data I built a spreadsheet which calculates the average correction for the autopilot, main compass and speed correction factor.

The autopilot needed to be 14.65 degrees larger value (so 238 degrees becomes 253 degrees).

The main compass will need to have a larger value by about 11.6 degrees which results in all but one of the adjustments being within 4 degrees with the exception of the one measurement of 7, that was repeated and found to be -1.  This will require physically moving the compass to match the autopilot.

It appears that matching the compass / autopilot on an autopilot course of 0, 11, 38, 187, 338 should be close. Then we can repeat.

I did adjust the autopilot in the slip tied up from 237/238 to 252/253 degrees (i.e. add 14) the system reported that the current swung compass has a maximum deviation of 7 degrees.

Other values in the autopilot configuration:

Rudder: 5
Rate: 2
Helm adjust looks good
Rudder limit: 30
Turn limit: 20
Cruise Speed: 7
Off course alarm: 20
Trim: 2
Remote: 1
Manual Type: 1
Drive Type: 3
Rudder: 1
Variation: Off
Auto Adapt: N
Lat N: was 52, now 33
Auto Release: Off
Wind Trim: 1
Response: 1

April 4, 2012: In the evening helped Lance Webb to get the steering shaft out of the CDi system on Princess Sierra sent shaft to Edson for addition of the stub shaft for a gear drive to connect to.

April 2, 2013: Installed Logitech K400 wireless keyboard onto the Lenovo q150 pc to make typing easier when writing log entries and other things which require extensive typing.

This keyboard has significantly more range, it works well in the saloon and forward part of the boat all the way into the forward cabin. The galley is good. The aft cabin is a bit spotty.

Note that the shift key and the up arrow are close together which results in some confusion. That will take a bit of getting used to. However, for what I want it should work quite well. The othe keyboard still works at the same time so I can  pick up either one.

April 1, 2013: Pickled watermaker 0.5 hr of runtime, total runtime on watermaker since new: hr 344.3

March 31, 2013: Easter Bunny at Isthmus

Getting ready to head back ro Redondo Beach. I had left the navigation system and AIS up and running all weekend to see how stable it was. At about 4am AIS stopped reporting on raytech. Powered down VHF radio which provides passive AIS reports... no change  only reports are from 4am. Cycled raytech software and then powered up radio (AIS source)-AIS reports are now fine fine.

Setting waypoint with Raytech software won't hold recycled raytech  software which cleared the issue.

Pre-Sail Checks: engine oil, gen oil, tran oil, antifreeze good. Engine hours: 990.7; Generator hours 3183.9

Had to power cycle rc320 all good.

1155 Startup Engine; oil 50psi

1200 Departed Isthmus heading back to King Harbor, Redondo Beach
bs5.1 sog5.7
cog 12 hd 357

Just beyond isthmus approach

sog 6.2 speed 5.8

main battery bank charging: -124 charging at 13a when first started charging saw 20a maximum.


sog 6.7 speed 6.2
150 true 9.6 knt3.6 bs sog 4.2
150 true 10.7 knts 4.45 bs 4.8 sog

Flying main and jib making 86 percent of polar performance, which is the consistent 15-20% loss for not having the staysail up.


8.0 wind 3.4 bs sog 3.8
313 hd 331 cog 8.5 wind 3.4 bs 3.6 sog
wind off port transom -150

1301 motoring again
         bs 6.8 sog 7.6 hd 355 cog 11
         bs 6.8 sog 7.6 cog 14 hd 358

1330 hrs bs 6.8 sog 7.4 cog 14 hd 359

1415 Ocean very calm, ocean glassy with only slight swell, no wind, between traffic separation scheme so current should be very stable. Used autopilot to change course 30 degrees at a time and recorded parameters. Will later use to determine the approximate current and then provide corrections.
Start bs 6.8 sog 7.1 cog 12 hd 355
+30 bs 6.8 sog 7.4 hd 25 cog 42
+30 bs 6.8 sog 7.5 hs 54 cog 70
+30 bs 6.8 sog 7.3 hd 85 cog 98
+30 bs 6.7 sog 7.2 hd 117 cog 124
+30 bs 6.7 sog 7.0 hd 148 cog 156
+30 bs 6.8 sog 6.8 hd 180 cog 184 mag176
+30 bs 6.8 sog 6.6 hd 200 cog 216 mag 207
+30 bs 6.7 sog 6.5 hd 235 cog 247 mag 239
+30 bs 6.7 sog 6.3 hd 264 cog 278 mag 270
+30 bs 6.8 og 6.3 hd 295 cog 310 mag 297
+30 bs 6.8 sog 6.6 hd 325 cog 344 mag 327
+30 bs 6.8 sog 7.0 hd 352 cog 16 mag 357
+30 bs 6.8 sog 7.4 hd 24 cog 45 mag 27
+30
bs 6.7 sog 7.5 hd 54 cog 70 mag 56
+30 bs 6.8 sog 7.5 hd 85 cog 98 mag 85
+30 bs 6.7 sog 7.3 hd 113 cog 124 mag 114
+30 bs 6.6 sog 6.9 hd 144 cog 154 mag 145
+30 bs 6.7 sog 6.8 hd 173 cog 184 mag 176
+30 bs 6.7 sog 6.3 hd 203 cog 214 mag 207
+30 bs 6.7 sog 6.4 hd 236 cog 247 mag 240
+30 bs 6.7 sog 6.0 hd 265 cog 278 mg 269
+30 bs 6.6 sog 6.1 hd 291 cog 312 mag 297
+30 bs 6.9 sog 6.5 hd 324 cog 344 mag 327
+30 bs 6.8 sog 7.0 hd 353 cog 15 mag 357
Emily's tummy is not happy!!! Going round and round with a slow swell and no wind did not do much for her motion sensitivity. 

1450 Heading back toward home

         bs 6.7 sog 7.0 hd 357 cog 16 mag 0
1545 At the R10 off Palos Verdes
1555 bs 6.9 sog 7.2 cog 31 hd 10 mag 13

1635 in slip
engine hr 985.0 (19 hr on oil)
gen has 11.5 hours on oil (intermittent hour meter 3183.9)

By 1730 everthing is put away except washing the boat.

Note: during cleanup found 0.25 inch steel ball bearing on port aft deck under outboard. not clear where it came from perhaps not even this boat (wishful thinking), [Later found out that this was from a fellow boater's sling shot, not part of the boat!]

Carefully cleaned engine and giving a good once over. Found slight transmission fluid leak from shift rod. a couple of drops on paper towel. A dark smuge under bell housing. may be valve cover gasket seap. cleaned up side of engine and bottom. too dark to be straight motor oil.

Tank Levels:
18.5 inches fuel remaining
17 inches water on main (port)
20 inches water on reserve (stbd) full

March 30, 2013:
On mooring C15 in Cherry Cove, in Isthmus Harbor. Visited with the Meistro's aboard Body Glove and had a wonderful tour of their wonderful vessel. Bobby Meistro is very proud of her, rightfully so!

Morning ran gen 0.5 hr

Afternoon ran gen 1.0 hr
Remaining fuel load 19.5 inch

2130 -98 ah to -78 ah, so one hour of generator run replaced about 20 amp hours. I am really looking forward to a new inverter/charger which should be able to supply perhaps 150 amp hours in an hour of charging time.

Transmission oil 1/4 inch above groove looks and smells good.

Note gen hour meter running again.

Evening ran gen 0.5 hr

March 29, 2013: Getting ready to head over to Catalina for Easter with the Corsair Yacht Club.

Filled water tanks 20 inches separated tanks

fuel 20.5 inches
gen 3192.6 stopped (9.5 hrs on oil)
engine 976.8 hrs (11 hrs on oil)
antifreeze good
pulled desicant out of engine room

The Raytech system needed one recycle on startup which is it's normal behavior with my odd seatalk bus.

Engine oil at full and golden; gen oil full and black

cleared harbor 1229

sog and bs identical at 6.9 knts
heading 207 cog 222 mag compass 210

1310 Past R10 Bouy off of Palos Verdes

         bs 6.8 sog 7.6 hd 158 cog 172

         bs6.8 sog 7.7 cog 179 hd 172

1345 Mid channel:

         bs 6.8 sog 7.2 cog 188 hd 177

near catalina motoring

         bs 6.88 sog 6.9 cog 191 hd 180

1550 Arrive Isthmus Approach

         bs 6.96 sog 7.1 cog 179 heading 165

Down on C15 Cherry Cove of Isthmus Harbor. A new Oyster 625 on B20 of Isthmus (Bandito).

March 26, 2013: Replaced o-rings on two inspection ports for large water tank. The two under port settee completed. Last time filling tank noticed slight leak on bolts supporting small table. will have to rebed when I change that o-ring.

Propane alarm went off. sensor appears to not like being on for days. Need to have seperate toggle switch for propane controller. Or just consider the sensors to be expendable. These sensors appear to "wear out" after a couple of years. It is worthwhile to have the sensor running all of the time in case there is a propane leak or other issue on the boat.

The failing hour meter for westerbeke generator may be part number 036192.

March 25, 2013: General Maintenance Evening: Installed covers on the terminals for the alternator diode splitter in the engine room; put new bilge pads under engine; ran generator 0.5 hrs now 9.5 hours on oil; hung desicant pack in engine room; pulled engine switch to remind to remove desicant before running engine.

March 24, 2013: Finished watermaker installation. In addition I made up membrane storage containers using 2" PVC pipe. On one end I welded a cap, on the other end a threaded fitting with a plug in that. Filling these containers with membrane biocide will help try to keep the spare membranes (which were part of a PUR 80 membrane stack which came with the boat but no drive motor). There are two membranes in that filter which are compatable with the PUR 40e. I have not tested them but in an emergency they might work for a period of time.

I did run the watermaker for two hours looking for leaks in the system.

It would be nice to find a replacement for the automatic valve to dump product water which has too much salt automatically over the side instead of going into the tank. Not absolutely necessary but nice to do at some point in time.

March 23, 2013: Day sail with Grubers. 

Pre-Sail Check: Motor oil and Transmission oil good; 976.0 engine hours; fuel load 20.5 inches.

1400 depart

1630 off malibu

1830 back in slip

976.9 hr on engine or about an hour for this trip.

March 3, 2012: Heading home from Cherry Cove

1030 One hour generator operation to charge batteries and pull down down the refrigerator. Generator hours now 3182.5 hrs.; Generator oil change was 3184.3 hours; looks like generator hour meter is intermittent and some digits are not always turning over; will replace hour meter. This intermittent behavior may explain higher than expected oil analysis numbers (not more than desired for an oil change just not consistent with the lower hours on the last oil change).

Total generator hours on this oil change approx 8 hours based upon hand logging of the hours.

1100 prep to head home. fuel 21.0 inches. oil good tx oil added 0.25 cup oil. looks like pink may be seaping braided fuel line between lif pump and secondary filter on engine

1115 Off mooring

         bs 5.33 sog 5.7 heading 352 cog 006
         bs 6.6 sog 6.8 heading 004 cog 013

Looks like need to add 13 degrees to compass

1200 The wind came up to 12 knts true, sailing! Making 95% polar with just main and jib up.

1230 staysail out speed up 10%: bs 6.3 sog 6.5

1400 Wind died so much for small craft warnings motoring 10 min to R10 then in

1455 in slip


engine 975.4 hrs
gen 3182.5 hrs

To verify that the generator hour meter has failed, ran gen at dock for half hour, the meter did not move. Verified power to hour meter. It is clear that the meter needs replaced

Verified that the diesel return line on main engine (Perkins) is the leak issue, pulled diesel fuel line due to leak at the end farthest from the engine (near the hard line returning to the fuel tank)

Keeping track of generator run time on oil change: approx 9 hours since oil change.


March 2, 2013: Heading for Cherry Cove for the weekend.

Pre-Sail Check: 968.4 engine hours at startup; 3182.4 hrs on generator; fuel 21.5 inches

0920 Depart for Cherry Cove

No wind; calm seas; motoring at 7 knts

Engine temp 165F, Oil Pressure 44psi

New ultrasonic knotmeter does not work wih second display hooked up directly to sensor. This did work with the older paddle wheel which I was doing just to determine if one of the displays was intermittent rather than the paddle wheel. Disconnnected second display and knotmeter works fine with the CS4500 knotmeter from Airmar!

Dripless stuffing box throwing a bit of carbon dust as it is wearing in. This is expected.

It is amazing how much the vibration levels are down with the straightend shaft, proper taper on the propeller  matched to the  shaft taper, and new cutless bearings.

Engine Room Check: Tinge of red on absorbant pads. Checked level of transmission fluid. Looks good. must have been in bilge when I put the pads down. Replaced pads. Wiped down transmission. Continue on. Checking bilge pads periodically. Note: Must shut down engine to check transmission oil level. There is a note online that there are rotating gears near the dipstick which hit the dipstick when it is not screwed down.

1200 engine room clean

         bring on root beer floats to celebrate!

Very flat water.  Boatspeed 7.05 sog 6.4 may be current will keep track.

1215 engine room clean

Checking calibration factor for speed. is 1.09 with new sensor assume more like default. now set to 1.00. speed+trip for 2 seconds. then cal displayed. press speed. use timer-reset to adjust. then speed+trip for 2 seconds.

1245 Engine Room Check: Looks like drip of ATF on end of transmission shift leaver. Wiped off one dot onto the paper towel.

speed 6.45 sog 6.2

1315 Engine Room Check: No drip on transmission shift leaver.


bs 6.44 sog 6.40-6.30 cog 186.0 hd 166.5

close to isthmus. sog 6.3-6.4 bs 6.44-6.5

1350 Picked up mooring C12 in Cherry Cove

Engine hours at shutdown: 973.0 hrs

One hour of generator operation in the evening. (8.5 hours of generator run on this oil change)

March 1, 2013: Battery watering and testing. Water level half way between plastic and the top of the plates on batteries, pretty uniform across the cells. Measured specific gravity of each cell prior to filling:
Forward, Starboard going aft
1.310
1.310
1.305

1.310
1.310
1.310

1.315
1.315
1.310

1.315
1.315
1.315

Forward, Port going aft
1.315
1.310
1.310

1.315
1.305
1.310

1.305
1.310
1.315

1.310
1.305
1.315